The weather continues to be unusual. It is the middle of April and it rained overnight into early morning. Winds are expected to start howling in the afternoon. I woke up at 6am to notice calm conditions so I was eager to fly this morning. 906MD’s starter had finally gotten so bad that it was nearly impossible to start it up. Also, COM2 hasn’t been working for a while so the plane has been grounded for maintenance. Fortunately 737GM was available but since it has been almost two weeks since I last flew, I texted Steve to see if he will join me for a couple of patterns around the airport before I fly solo to Byron, Tracy and back. He was available and we decided to meet at 8:30am. On the way to the airport, I checked AWOS to note that there was a 7kts wind from 240 at Livermore, 9kts from 220 at Byron and 11 its at Tracy from 260.
737GM wasn’t easy to start either. It took a number of primes and then a number of throttle primes. We pushed the throttle fully in and kept pumping it while the engine continued to sputter. It gradually picked up RPM and was finally able to idle around 700rpm.
We did 4 patterns around Livermore before Steve declared that he had had enough and decided to get dropped off at the northwest tiedowns while I kept the engine running and continued on a solo. Two things I noticed are (1) that the throttle lever is significantly shorter compared to the one on 906MD and (2) that the throttle lever slips out very easily when the friction lock is not engaged. A couple of times I took my hand off the throttle to adjust trim and the engine rpm dropped as indicated by a change in the hum. Steve and I both lunged for the throttle at the same time to push it back in.
I got a clearance for right downwind on 25R and as I flew towards Brushy Peak, it got significantly bumpier. Clearly the winds were stronger the higher I flew. I chickened out and asked Tower to bring me back in for 25R. I appreciated that the Tower thought there might be a problem and asked if I need any assistance. It continued to be windy and bumpy but not terribly problematic so I did 4 touch and go’s back at Livermore before calling it quits.
